Underwater Propeller Change, USS Enterprise, CVN-65

US Navy Divers Remove the Propeller
After the boss nut was broken off, the shaft
threads were checked and chased. All appeared to be in perfect condition. The
threads were cleaned and wrapped with a 9 thread line. The entire shaft was
then covered with canvas and a thin protective sleeve. A large diameter wire
rope grommets and 2-1/2 inch shackles were attached in each of the propeller
lifting shell fittings. A snatch block and a tight grip wire were attached to
the after fitting in preparation for rigging the 50 ton chain hoists. Propeller
removing studs were machined down 0.040 of an inch and installed. (This allowed
water to flow out of the huge threads without building up what we called
Hydraulic Lock. Seawater doesn't compress, and if you don't give the water some
place to go, it builds up enough pressure to prevent screwing bolts into their
threaded holes.)
Two 50-ton chain hoist were placed on board
the barge by the pier crane. The barge was then repositioned alongside
Enterprise in line with frame to 228, where a tight grip wire was
attached to the Enterprise after hull fitting. One snatch block was
attached at the Enterprise after hull fitting and two additional snatch
blocks were attached on the barge deck. Line's rigged through the snatch blocks
were controlled by grip hoiss located on the barge. The 50-ton chain hoist was
then hooked on to the tight grip wire which would support its way and guide its
movement. Once in the vicinity of the after hull fitting it was disconnected
from the tight grip wire and lowered so it could be attached to the grommet and
shackle which was already on the after all fitting. The procedure was repeated
to locate the other 50-ton chain hoist temporarily on the after all fitting.
The shaft was then jacked over to position the propeller studs at 3 and 9
o'clock.
The pilgrim nut method was chosen for
unseating the propeller after learning from NAVSEA that an excess of 700 tons
of force would be required to unseat the propeller from the shaft. Preparations
were made to install the pilgrim nut on the shaft and the backing played on the
propeller stunts as soon as the backing plate had arrived from Puget Sound
naval shipyard. The pilgrim nut was tested pier side using a 10 ton concrete
block. The barge was then positioned alongside the carrier and the pilgrim nut
was yard and stayed into position on the propeller shaft. The backing plate
followed into its position on the propeller studs. The stud nuts were installed
on the propeller studs, the pilgrim nut was tightened, and 4 by 6 inch wooden
blocks were placed at 3 and 9 o'clock positions to absorb some of the impact
when the propeller was unseated. 10,000 PSI of pressure was applied to the
pilgrim nut to break the propeller free from the shaft taper. The propeller
moved one inch along the shaft in two extensions of the pilgrim nut. The studs,
nuts, backing plate and pilgrim nut were then removed.
The damaged Enterprise propeller was
removed by the yard and stayed method from the forward to after air hoist. Once
off the shaft, the propeller was positioned alongside the barge. It was
suspended on the 50-ton air hoist which had been connected to the propeller
balance beam. The barge was warped to within reach of the YD 116 floating
crane, which hooked on to the propeller, lifted it from the barge balance laid
it down on the pier. The propeller studs were then removed and lifting eyes in
installed so it could be lifted onto the flatbed truck. The impact from the
grounding had reduced the distance across the propeller blade tips from 21 to
17 feet. After underwater inspection of the other Enterprise propellers
the #1 shaft was inspected to verify that there had been no damage during
removal of the old propeller. The shaft taper runout was checked using dial
indicators. A mounting fixture was especially fabricated to fit on the strut
barrel and hold the three dial indicators. The shaft was then jacked over and
readings taken at designated 12,3, 6, 9 o'clock positions and ending again at
the 12 o'clock position. Shaft alignment was satisfactory.
WebMaster Bruce |